Clayton Armstrong 2011-02-22 GSK Aranda SP - steam&condensat
STEAM AND CONDENSATE AUDIT
Project N°30275
Date: 04/02/2011
GSK MANUFACTURING Aranda, Spain
Page 33 of 45
Established by E. Morin
To the attention of Ms. Beatriz Herrero-Gonzalo
8 Complete check list of all verifications done during the audit
Potential optimisation
Status
Comments
STEAM GENERATION
Steam pressure setting
OK
7 barg is good compromise. 6 barg would certainly
be too low for distribution (lines sizing restrictions)
Feed water temp. to the boilers
OK
93°C measured on the feedwater pump. Clayton
requires a minimum of 90°C
Stack temperature in front of
NA
Not possible to measure on Clayton boilers.
economizer
Stack temperature after economizer
OK
Refer to combustion analysis or temperatures
reported in the BMS system (when repaired)
Combustion air temperature
To be improved
Ambient
Oxygen rate
OK
5-7% depending on the firing rate
Boiler sizing
OK
Boiler blow down rate
To be improved
Could be reduced to fit with Clayton
recommendations
Refer to optimization project n°1
Deaerator pressure
NA
Atmospheric feedwater tank
Feed-water pre-heating
NA
Boiler stand-by time and volatility of
OK
Clayton steam generators have a good response
steam demand
for these conditions
Boiler blow-down recovery
NA
Blowdown is too low at current steam demand to
recover energy within 5 years payback
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