Clayton Armstrong 2011-02-22 GSK Aranda SP - steam&condensat
STEAM AND CONDENSATE AUDIT
Project N°30275
Date: 04/02/2011
GSK MANUFACTURING Aranda, Spain
Page 18 of 45
Established by E. Morin
To the attention of Ms. Beatriz Herrero-Gonzalo
Water savings
Existing
Proposed
Savings
Flash steam flow estimated
kg/h
0,059
0,045
0,015
Yearly water lost
m³/year
371
278
Water unit costs
€/m3
5,0
5,0
Water costs
€/yr
1853
1390
463
The total savings would be 2340 €/year .
2. Solution 2 : Move the condensate connections to the bottom of the tank with a sparger tube
The modification will imply an increase of the feedwater temperature pumped to the generators.
We estimate this increase at 5°C. The efficiency gain on steam production will be about 0.5%.
Boiler efficiency
Existing
Proposed
Savings
Feedwater temperature °C
93,0
98,0
Boiler efficiency
%
86,0
86,5
0,5
Fuel savings
Existing
Proposed
Savings
yearly Energy used
GJ/yr
12499,2
12499
Boiler efficiency
%
86,0
86,5
0,5
Fuel used
MWh/yr hhv
4486
4460
25,93
Fuel unit costs
€/MWh hhv
25,0
25,0
Fuel costs
€/year
112145
111496
648
CO2 savings
Existing
Proposed
Savings
Energy used
Gj/yr
16149
16055
93
CO2 emissions
kg CO2/GJ
50,6
51
CO2 produced
t/yr
817
812
5
Savings are poor (less than 1000 €) because steam production is very low. If the steam demand
increases, savings will follow.
Made with FlippingBook Digital Publishing Software